I Got the Triumph Running

It’s time for an update, and it’s a good one. After a surprisingly short amount of work, I got the Triumph running, and running somewhat better than I expected. I regret not taking any pictures during the process, but it wasn’t really that exciting. I have a few things to address before the car is road-ready, but they shouldn’t present much trouble.

The first thing I did was remove the alternator and take it to a local place for a rebuild. Last time I was working on the car, I hooked up a jump pack backwards and smoke came out of the alternator. After taking it off and spinning it, I found the bearings a little stiff, so it was probably time for a refreshing anyways.

Next, I replaced the head gasket. I figured the gasket needed replacing due to a compression test from the last time I worked on the car. All the cylinders had compression, but it was low and very inconsistent. I expected to need most of the day to prep the head for removal; in fact, it took barely over an hour. I was ready to remove the head at around 11:30am, but no one was around to help me (with both manifolds attached it probably weighs 70-100 pounds). So I decided to work on something else I’ve been meaning to get to.

I’ve wanted to remove the engine-powered cooling fan and replace it with an electric fan for quite a while. I’ve had a fan and a controller kit, plus an engine fan eliminator kit ready to go for a few years. While waiting for my wife to get home to help with the head, I went ahead with the electric fan installation. The fan I bought was too thick to use as a puller behind the radiator, but luckily it was reversible, and thus easily mountable on the front of the radiator. I used the supplied zip ties to mount the fan to the radiator, and then connected the controller. After getting the car running, I discovered two problems with the controller: one, connecting it to the ignition coil doesn’t provide enough power, so I’ll probably connect it straight to the battery; two, the included push-in probe that sticks in the radiator fins sucks and doesn’t with with my radiator. I ordered a screw in replacement that I’ll put in a metal tee in the upper radiator hose.

I still had some time leftover, so I gave the carburetors a quick clean up and refresh and bought some supplies like coolant and a battery.

Once my wife got home, we took the head off, and to my surprise the gasket appeared to be in fine shape. I was expecting a missing chunk or something like last time. The block appeared in good shape also, and so did the head and all the valves. I don’t have a straight edge, so I didn’t check flatness, but I don’t think it’s an issue; I’ve never had coolant and oil mixing. I put the new gasket on and we set the head down on it. The next day I took maybe two hours or so to button it up.

Once everything was bolted together and filled up and plugged in, it was time to fire up the car. It took maybe half an hour of trying to get the car started, and when it did finally get going, it would only stay running with my foot holding the throttle open slightly. Yesterday, I mostly fixed the hard starting problem by adjusting the choke, which wasn’t doing anything at all. Now the car will run unattended, but only with the choke on. That seems to point to some kind of vacuum leak. I tried to track one down last time, but to no avail. Currently, my top potential culprits are the EGR valve, which I plan on eliminating, or the rocker cover, which is kind of out of shape. I plan to address that with a bit of RTV silicone. Hopefully that will take care of things and I can get the car registered and on the road in a week or two. I’ll be sure to add some pictures to the next post.

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